富水砂层地铁竖井横通道注浆加固施工方案研究
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作者单位:

1.中铁隧道局集团(上海)特种高新技术有限公司,上海 201306 ;2.郑州城建职业学院,河南 郑州 450001

作者简介:

倪汉杰(1991—),男,工程师,从事隧道及地下工程注浆加固方面的施工及管理工作。

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中图分类号:

U231+.3

基金项目:

河南省科技厅自然科学基金资助项目(162102210188);河南省建筑业协会科研开发项目(YJX-2023-K01、YJX-2023-K02)


Study on the construction program of grouting reinforcement for subway shaft cross passage in water-rich sand layer
Author:
Affiliation:

1.China Railway Tunnel Bureau Group (Shanghai) Special High-Tech Company Limited, Shanghai, 201306 , China ;2. Zhengzhou Urban Construction Vocational College, Zhengzhou 450001 , Henan, China

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    摘要:

    为解决饱和粉细砂地层注浆加固施工过程中地表构筑物变形明显、浆液扩散效果差的问题,文章以广州地铁 13号线西场站工程为研究背景,针对富水砂层注浆加固施工工艺优化、注浆加固材料的适用性开展现场试验对比研究。结果表明:1)采用水平钻杆后退式注浆工艺,在注浆孔周边打设泄压孔进行真空抽吸,在注浆压力与排水压力的共同作用下能够实现定向诱导渗透注浆;2)在超细水泥添加减水剂能够提升浆液的渗透能力,同等注浆压力条件下,添加 0.4%减水剂的单孔注浆量比未添加减水剂的单孔注浆量提升 4倍;现场施工监测结果表明, 采用“抽注法”注浆,在不提高注浆压力的前提下,可以有效控制周边地层变形,地表和管线的隆起变形值均控制在 1cm以内。本文研究结果可为类似工程提供一定参考。

    Abstract:

    In order to solve the problem of obvious deformation of surface structures and poor spreading effect of slurry during the construction of grouting reinforcement in saturated fine sand strata, taking Guangzhou metro line 13 Xiba station project as the research background, on-site experimental comparative research is carried out on the optimization of the construction process of grouting reinforcement of water-rich sand strata and the applicability of grouting reinforcement materials. The results show that: 1) the use of horizontal drilling rod backward grouting process, in the periphery of grouting holes to set up pressure relief holes for vacuum suction, grouting pressure and drainage pressure under the joint action of the grouting pressure can be realized under the direction of the induced infiltration of grouting; 2) in the ultra-fine cement to add water reducer can enhance the penetration capacity of the slurry, the same conditions of the grouting pressure, the addition of $0.4\%$ of the single-hole grouting volume than the addition of a single-hole grouting volume of the single-hole grouting volume of the water reducer to increase by 4 times; on-site monitoring results show that the use of The field construction monitoring results show that the grouting by "pumping method" can effectively control the deformation of the surrounding strata without increasing the grouting pressure, and the uplift deformation values of the ground surface and pipeline are controlled within 1cm . The results of this paper can provide certain reference for similar projects.

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倪汉杰,张鹏,王远六,易领兵,邓康康.富水砂层地铁竖井横通道注浆加固施工方案研究[J].工程建设,2025,57(10):23-30

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  • 收稿日期:2025-02-26
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  • 在线发布日期: 2025-11-06
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